Well if no one knows iv been having a problom with my car latly. I finly came down to it being timing. So iv been working with the timing for 3 days now trying to get it running good. Well today I had a brake thru with the car and got it running good. And I mean good like I got a 3rd gear chrp out of it, It was awsome. Well it ran good for about 30mins then sterted missing again and getting harder and harder to start. To now it wont start at all... What can this be???
__________________
1990 Mustang LX, 2.3T, 2.5 Intercooler Piping, Front Mount Intercooler, Ported And Polished Upper And Lower Intake, BBK T/B, Ported And Polished Big Valve Head, Ranger Roller Cam And Roller Rockers, Forged Pistons And Rods, 8.8 Rearend, 373 Gears, BBK Short Throw Shifter, And A Few More Mods Ill Keep To My Self ;-)
Also the car useily has like 40psi of presure and now it only has 20psi? I was told that a bad ECT will do that but the ECU is not throwing that code.
__________________
1990 Mustang LX, 2.3T, 2.5 Intercooler Piping, Front Mount Intercooler, Ported And Polished Upper And Lower Intake, BBK T/B, Ported And Polished Big Valve Head, Ranger Roller Cam And Roller Rockers, Forged Pistons And Rods, 8.8 Rearend, 373 Gears, BBK Short Throw Shifter, And A Few More Mods Ill Keep To My Self ;-)
Also the car useily has like 40psi of presure and now it only has 20psi? I was told that a bad ECT will do that but the ECU is not throwing that code.
It is throwing codes:
22
23
81
82
__________________
1990 Mustang LX, 2.3T, 2.5 Intercooler Piping, Front Mount Intercooler, Ported And Polished Upper And Lower Intake, BBK T/B, Ported And Polished Big Valve Head, Ranger Roller Cam And Roller Rockers, Forged Pistons And Rods, 8.8 Rearend, 373 Gears, BBK Short Throw Shifter, And A Few More Mods Ill Keep To My Self ;-)
you may have also advanced the timing to far, with the spout connector off did you time it ? and to what degree? fuel pump or fuel filter may be bad...
__________________
DSS 331 stroker, AFR 185 heads, Performer rpm 2 intake, Accufab 75 mm race TB, 30lb injectors, 80 mm Pro-M mass air, Extreme energy cam 266.
Anderson ford power pipe the big one, Ford motor sport shorty headers, Bassani x pipe custom cat back with flows, World class T5, center force duel friction clutch.
New pump and filter. And Like I said the car ran awsome for like 15-20mins.
__________________
1990 Mustang LX, 2.3T, 2.5 Intercooler Piping, Front Mount Intercooler, Ported And Polished Upper And Lower Intake, BBK T/B, Ported And Polished Big Valve Head, Ranger Roller Cam And Roller Rockers, Forged Pistons And Rods, 8.8 Rearend, 373 Gears, BBK Short Throw Shifter, And A Few More Mods Ill Keep To My Self ;-)
may be something due to the fuel pump connection or pump itself.
__________________
DSS 331 stroker, AFR 185 heads, Performer rpm 2 intake, Accufab 75 mm race TB, 30lb injectors, 80 mm Pro-M mass air, Extreme energy cam 266.
Anderson ford power pipe the big one, Ford motor sport shorty headers, Bassani x pipe custom cat back with flows, World class T5, center force duel friction clutch.
22 - MAP sensor or BARO. sensor out of range
23 - TPS out of range (throttle position sensor)
81 - AIR diverter solenoid fault (air pump issues maybe)
82 - AIR diverter solenoid circuit fault
it sounds like you might need to adjust or replace your TP sensor, that may be much of the problem. have you done anything with your AIR pump? the 81 and 82 codes are not a big deal, maybe you elimintated the system. the MAP sensor and TP sensor are important though.
Oh, and that code 82 could also be the "integrated relay control module" but I dont know anything about that and I dont think its likely.
__________________
89' GT Ragtop.
-==-
Ford Racing "C" springs
SLP Loudmouths
Summit o/r x-pipe
BBK equal length headers
BBK strut tower brace
Chipped by DynoSources
-==-
1990 Mustang LX, 2.3T, 2.5 Intercooler Piping, Front Mount Intercooler, Ported And Polished Upper And Lower Intake, BBK T/B, Ported And Polished Big Valve Head, Ranger Roller Cam And Roller Rockers, Forged Pistons And Rods, 8.8 Rearend, 373 Gears, BBK Short Throw Shifter, And A Few More Mods Ill Keep To My Self ;-)
Ok so alittle while ago I made a joke that maybe the car ran out of gas. Well I was right, the car was out of gas. ( now please dont laugh). Ok so it is running but the idle is high and it smells very rich. So tomarrow I will put new plugs in and try to dizzy time it with a light.
__________________
1990 Mustang LX, 2.3T, 2.5 Intercooler Piping, Front Mount Intercooler, Ported And Polished Upper And Lower Intake, BBK T/B, Ported And Polished Big Valve Head, Ranger Roller Cam And Roller Rockers, Forged Pistons And Rods, 8.8 Rearend, 373 Gears, BBK Short Throw Shifter, And A Few More Mods Ill Keep To My Self ;-)